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EuropaOwners N914XL - Bob Borger, N.Texas, USA: 99.0 hrs - Subsequent Flights Album has been updated as of 2016 05 16. Subsequent Flights
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N914XL - Bob Borger, N.Texas, USA: 99.0 hrs - Subsequent Flights Album has been updated as of 2016 05 16.

1. DSC_0064 2. First Flight 3. Subsequent ... 4. Tri-Gear... 5. Weight... 6. Aviation... 7. OSHKOSH 2007 ... 46. Fuel Tank...

Random Images

DSCN5574Ann

DSCN5574Ann

Date: 02/25/2007 Views: 3846

Starboard wing 59.

Starboard wing 59.

Date: 06/19/2009 Views: 4652

IMG_0057

IMG_0057

Date: 03/03/2007 Views: 11445

Newest Image

EAA SITE

EAA SITE

Date: 08/23/2023 Views: 693384

Subsequent Flights

I've been delinquent in my posts. I'll add some pictures of the aircraft as I have been flying it. And I'll add some pictures of North Texas from the last flights.

Date: 02/13/2009
Owner: rlborger
Size: 77 items (123 items total)
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IMG_0858post

IMG_0858post

We also put the graphics on his aircraft.

Date: 01/22/2010
Views: 3981
IMG_0866post

IMG_0866post

Yup, that's Mighty Mouse. That was Gary's nick-name in the Navy. So it's fitting for the name of his Toot.

Date: 01/22/2010
Views: 3976
IMG_0868post

IMG_0868post

We completed the metal installation as well as some radio wiring work and the graphics. I had hoped to work on my coolant leak today (23rd) but it's raining. Maybe tomorrow...

Date: 01/22/2010
Views: 4058
IMG_0870post

IMG_0870post

2010 01 24 Went to the hanger to work on the coolant leak. Pulled the aircraft out, chocked it and tied the tail to the fence.

Date: 01/24/2010
Views: 4131
IMG_0869

IMG_0869

Started the engine and let it run a bit and settle down. Started looking for signs of a leak. Took a bit, but finally found some coolant drops.

Date: 01/24/2010
Views: 3595
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IMG_0872post

First found them here.

Date: 01/24/2010
Views: 3989
IMG_0873post

IMG_0873post

Then saw the drop on the engine mount cross-tube and saw more coming across the tube.

Date: 01/24/2010
Views: 4511
IMG_0874post

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Finally, back underneath to find the old drops on the cross tube and there was the tell-tale residue of evaporated coolant on the intake to the coolant pump (Green arrow). Shut things down. Found the longest screwdriver I had and was able to reach the c

Date: 01/24/2010
Views: 5014
IMG_0876post

IMG_0876post

Put the aircraft back in the hanger and put the cowl back on to wait for a better day to fly.

Date: 01/24/2010
Views: 4848
IMG_0877post

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Because today it was a 30 degree X-wind gusting to 25 kts. Too much for me at this time. Maybe in another 10 - 15 hours... Might be good flying weather tomorrow after work. We'll see.

Date: 01/24/2010
Views: 4214
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