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EuropaOwners N914XL - Bob Borger, N.Texas, USA: 99.0 hrs - Subsequent Flights Album has been updated as of 2016 05 16. Tri-Gear Conversion
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N914XL - Bob Borger, N.Texas, USA: 99.0 hrs - Subsequent Flights Album has been updated as of 2016 05 16.

1. DSC_0064 2. First Flight 3. Subsequent ... 4. Tri-Gear... 5. Weight... 6. Aviation... 7. OSHKOSH 2007 ... 46. Fuel Tank...

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DSCN5349Ann

DSCN5349Ann

Date: 12/28/2006 Views: 4680

046_G

046_G

Date: 07/19/2007 Views: 4870

24112006020_G

24112006020_G

Date: 11/26/2006 Views: 4784

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EAA SITE

EAA SITE

Date: 08/23/2023 Views: 693380

Tri-Gear Conversion

After being blown off the runway on takeoff and into a ground loop at 40 kts, it has been decided to convert the aircraft from Monowheel to Tri-gear. This album documents this conversion and repair work. The album is not comprehensive as I often was up to my elbows in epoxy, fiberglas, Araldite and other nasty things when I would have wanted a picture or two. Still, you should be able to get an idea of what was involved. Work has almost been completed. The aircraft is flying again. Remaining work is to make interference fairings for the landing gear leg fairings to the wheel pants and body. I'll put the wheel pants on tomorrow and see how it goes. Without any go-fast fairings it does 110 KTS at 5000 RPM, 28 in MP & 3.6 gph.

Date: 10/02/2010
Owner: rlborger
Size: 345 items
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IMG_3327em

IMG_3327em

Next request was for a compression check. 80/80, 80/80, 80/80, 79/80. No problem there. But while doing this I decided to check the plugs. Cylinder #3 plugs looked different. WHY?

Date: 06/12/2012
Views: 6118
IMG_3331em

IMG_3331em

Turn the plugs over and one plug on #3 looks funny. Calls for a closer look...

Date: 06/12/2012
Views: 5070
IMG_3332em

IMG_3332em

Looks like that plug had been bumped some time during transport. Porcelain shows a crack. OK, replaced ALL the plugs. Engine still didn't run right.

Date: 06/12/2012
Views: 6803
IMG_3334post

IMG_3334post

Requests to check the fuel delivery system. Started with the gascolator. Any large quantity of crap in the gascolator? Here's the fuel from the gascolator in the test vessel. A tiny bit of black crud from who knows what. But not enough to cause a pro

Date: 06/13/2012
Views: 5034
IMG_3367post

IMG_3367post

Request for fuel pressure input to the fuel pressure regulator. Installed a fuel pressure sensor on the input to the regulator. So now we have differential pressure out of the regulator and pressure into the regulator.

Date: 07/02/2012
Views: 5137
IMG_3374em

IMG_3374em

Run the engine, check the pressures. All seems OK. 5 lbs into the regulator and 3.8 lbs out of the regulator. This is with the Billet mechanical pump. Which became the next source of concern.

Date: 07/04/2012
Views: 4918
IMG_3384em

IMG_3384em

Remove the Billet pump from the circuit. Run with only electric pump. Input line connected directly to the regulator. At the same time, remove airbox pressure from differential gauge to get absolute fuel pressure out of regulator.

Date: 07/09/2012
Views: 5873
IMG_3392

IMG_3392

Differential pressure with engine running on electric pump: 3.8 lbs

Date: 07/09/2012
Views: 5595
IMG_3391em

IMG_3391em

Input fuel pressure: 5 lbs. Just like with the Billet pump. Next request was for a fuel flow test. Reconnected the Billet pump to the fuel circult. One electric pump running fuel through the billet pump produced 1 gallon of fuel in a bit less than 3 m

Date: 07/09/2012
Views: 7930
IMG_3438em

IMG_3438em

There was a bit more work with the Billet pump package, but it proved not to be the problem. Moving on, OK, not the fuel system. Try running the engine as a normally aspirated engine. Remove the connection between the turbo and airbox. Believe it or

Date: 07/17/2012
Views: 7767
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